Come on Baby, Light my Fire! |
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| The Coed Cae B&B journey to sustainable heating | |
Spring 2008 In particular a heating bore. Well not so much heating, as the peculiarities of trying to marry thermal storage technology to solar heating circuitry whilst maintaining ...and there I go again. |
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| The Plan | |
The seeds of the project were germinated in the dirt of our old heating system, and since this was a solid fuel Rayburn which produced dust by the kilogram this is no allegorical reference. I have to say I had a grudging respect for the old range, for all its drawbacks. It gave a real character to the kitchen, which is pretty much the hub of our lives, and provided a warm retreat through the cold winter months. The problems really came to light during spring and autumn, when we needed the heating on, but it wasn't that cold. At this time the kitchen became unbearably hot, and guests would see us serving breakfast in shorts and t-shirts, sweat lashing out, whilst they were reaching for jumpers. Another slight problem was that it didn't heat the house, and what heat it did give out peaked about 3 hours after the last fuelling. Typically this meant that the house was at its warmest at 2:00 a.m and 10:00 a.m. which was far from ideal. |
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| Paying for it | |
There were no two ways about it, this was to be an expensive venture. As well as the heating hardware, we needed to build a boiler house to enclose it, and a series of dry log stores for the fuel. Fortunately at the time, various streams of funding were available to help with the installation of carbon-neutral technology. We had been working on the principle of installing a system to which we could add solar water heating at a later date, but in the end bundled the lot together on the application. The form filling for a business application was quite a task, it being the same form as a health trust would fill in to convert their hospitals, and we failed on our first attempt. Given that you are only permitted two application attempts this was a blow, but we addressed the problems, reapplied and were successful. The grant only applied to the specific technology (i.e. the boiler and panels, but not the boiler house or the plumbing required to attach to an existing heating circuit) and covered about half of the cost. |
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| Installation | |
One of the stipulations of the grant was that installation be carried out by an accredited engineer, and by chance we noticed that one of them The Green Heat Team was based about 4 miles up the road in Dolgellau. We were aware that they were a fairly new business with only a few installations under their belt, but mindful of the leaps of faith given to us over the years and the potential benefits of dealing with a local firm, we decided to go with them. We had scheduled the installation for late autumn, it being a quiet time for the B&B, and the switch from Rayburn to log boiler occurred just before Christmas. On commissioning the new system, it was immediately obvious that things were not going as planned. The lack of background experience of the Green heat team had been a concern, but turned out to be a red herring; the technology itself, or the way we were using it, was sufficiently new that when we ran into problems even the importers of the hardware were floundering and giving different answers each time we spoke. In the end, most technical problems were ironed out around the kitchen table with ourselves, Andy from GHT and large piles of scrap paper. In order to make any kind of valid contribution to the discussion we had to get up to speed on conventional heating systems, then bin much of what we had learned as we got to grips with the new technology. I think that it was around this point we became boring. Christmas was spent with clip-board and/or thermometer in hand checking various parameters, or trying to explain the system to anyone prepared to listen (in itself a dwindling supply). Because we were effectively making it up as we went along, it took time changing settings and logging the effects on the system. Slowly but surely we ironed out the problems, redesigning bits along the way when required until the system was fully active. Not withstanding the pressure of needing the place heated for B&B guests whilst working around an unfamiliar system, the whole process of design, installation and troubleshooting has been strangely satisfying, and to be honest, I think we ended up with a better system than we initially specified. To a large part that would be because the original design didn’t work, but if it had worked, what we ended up with is better. Details of the system itself, problems experienced along the way, and various redesigns are detailed below lest you become as nerdy as us! |
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| The system | |
The heating system was designed around thermal store technology. In this set-up a huge insulated Akvaterm accumulator tank containing 1500 litres of water acts as a heat store that can be added to or drawn upon, much like a rechargeable battery. Heat In Heat Out So far so good. Or not, as the case may be. | |
| Problems | |
When the stratification was breaking down, there seemed very little help to be found from the equipment suppliers. A particular low point (both for us and the GHT) was when we hit the answer “well, storage technology doesn’t really work that well on radiator systems, it is much better for under-floor heating which work at a lower temperature”. Great! Nobody was putting that in their adverts! Anyway, at this point, with no intention of re-plumbing the entire house and with a strong stubborn streak, we set about MAKING it work. But first I need to acquaint you with the heating circuit plumbing into the storage tank. The hot water is drawn from the top and returns to the bottom. In an ideal world where stratification is maintained, hot water is drawn off at the top, loses its heat in the house, and returns cold to the bottom. If warm water is returned to the bottom of the tank, it messes things up pretty quickly. We figured that the hot water needed as much an opportunity to lose its heat as possible, and the longer it was in the heating circuit, the more heat loss would occur. With this in mind we set the circulation pump on its slowest setting and it instantly improved things. However, the heat loss ultimately depends on the demands being placed on it by the system, and if most of the radiators are turned off, the water may still return hot. There is a further feature to the plumbing; the outflow and return pipes are bridged by a shunt so that the pipework resembles a letter H turned on its side. The shunt is controlled by a ThermOmatic K valve which redirects hot return water through the shunt and back around the heating circuit rather than allowing it into the bottom of the tank. This again minimises the disturbance to the tank strata. There was a whole set of issues relating to this valve, mainly associated with where to place the temperature probe. The received wisdom was to have the probe stabilising the outflow temperature. We batted this one around until our heads hurt, and, no longer placing much value on received wisdom, tried various positions and settings. We currently have it on the return pipe, set at 55 oC, so if the water returns above that temp, it gets sent around the system again. The idea behind this is that when the hotter water is used up, the whole tank still contains serviceable domestic hot water (DHW), which is important to our B&B guests. However, this still left a lot of warm water at the bottom of the tank. To make better use of this, and to further stabilize the stratification, the DHW was re-routed through a heat-exchange coil at the bottom of the tank before it passed through the normal coil at the top. In this way the cold mains-feed water was preheated by the cooler water at the bottom of the tank then topped up by the hot water at the top. This constantly works to re-establish the stratification by taking heat primarily from the bottom of the tank. Because the solar was getting little opportunity to contribute to
the accumulator tank, we decided to change tack and use it to further
pre-heat the DHW. This meant a separate dedicated tank (250 litre,
I think) for the solar heating. The DHW was sent through a heat exchange
at the top of the solar tank before heading off to the accumulator
tank. By being first in the pre-heat sequence, and therefore exposed
to cold water every time a hot tap is turned on, the heat in the solar
tank is quickly removed, and thus the tank is kept relatively cool.
This means that the panels have to heat up less before the system
is activated, and so even on fairly overcast winter’s days the
panels are contributing. The problem with the shower was resolved by the installation of flow reducing washers in the pipe work, and the leaky joint problem (arguably the most stressful of all) was resolved by waiting for damp patches to appear, and watching in horror as water lapped around the computer on the office floor. The system still loses pressure over time, so I'm not convinced there isn't another leak out there somewhere. Ah well, it can't all be brilliant! |
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| Update November 2008 | |
As we roll towards our first full winter (which arguably started early September), a few issues are worth adding into the pot.
The ThermOmatic K probe is currently on the outflow and set at about 60oC. Having messed around with this in various settings, it seems like on the outflow works best if you have a high tank temperature, whilst on the return seems to make the most of a lower temperature tank situation. I guess you pays your money and you takes your choice! Another nasty surprise came in the form of our wood fuel stores. The plan was that we hold a years worth of fuel (about 30 cubic metres) on site and we work through it in simple rotation. However, we have recently discovered that much of the oak which has been seasoning undercover for 12 months is still too wet to burn. Fortunately, we have some pine from the same time which is fully seasoned, but this has meant digging into the (mixed) log store in various positions to locate it. Bang goes our simple store rotation, along with any notion that a year is enough to season oak. I am currently logging some large oak trunks which have been cut for at least a couple of years, to the extent that the bark has mostly fallen away and the outer couple of centimeters are rotten in places. Yet when I split these logs, I am constantly sprayed in the face with sap from the sound wood beneath. Irrespective of the felling time, it seems like the seasoning process only really gets going once the logs have been split. In answer to these problems, we have built a further large log-store, taking us towards a two year stock, and are working hard to fill it ASAP. Additionally, I have been making a conscious effort to split logs smaller, and to split smaller logs, giving it all a better chance of seasoning quickly.
My understanding is that they will probably leave us for a quieter hibernation spot over winter, and we look forward to seeing them again next summer. | |
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